JPS5833283B2 - Blast furnace operation method - Google Patents
Blast furnace operation methodInfo
- Publication number
- JPS5833283B2 JPS5833283B2 JP55014835A JP1483580A JPS5833283B2 JP S5833283 B2 JPS5833283 B2 JP S5833283B2 JP 55014835 A JP55014835 A JP 55014835A JP 1483580 A JP1483580 A JP 1483580A JP S5833283 B2 JPS5833283 B2 JP S5833283B2
- Authority
- JP
- Japan
- Prior art keywords
- level
- furnace
- charge
- blast furnace
- shaft
- Prior art date
- Legal status (The legal status is an assumption and is not a legal conclusion. Google has not performed a legal analysis and makes no representation as to the accuracy of the status listed.)
- Expired
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Classifications
-
- C—CHEMISTRY; METALLURGY
- C21—METALLURGY OF IRON
- C21B—MANUFACTURE OF IRON OR STEEL
- C21B5/00—Making pig-iron in the blast furnace
- C21B5/006—Automatically controlling the process
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- Engineering & Computer Science (AREA)
- Chemical & Material Sciences (AREA)
- Manufacturing & Machinery (AREA)
- Materials Engineering (AREA)
- Metallurgy (AREA)
- Organic Chemistry (AREA)
- Blast Furnaces (AREA)
Description
【発明の詳細な説明】 本発明は高炉操業法に関するものである。[Detailed description of the invention] The present invention relates to a blast furnace operating method.
而して本発明の第1の目的は高炉を休風することなく円
周バランスの崩れた融着帯を速やかに回復させ、銑中(
Si)のバラツキ減少、高炉燃料比の低下などを図れ、
る高炉操業法を提供せんとするものである。Therefore, the first object of the present invention is to quickly restore the cohesive zone which has lost its circumferential balance without having to take a break from the blast furnace.
Reduce the variation in Si), lower the blast furnace fuel ratio, etc.
The aim is to provide a method for operating a blast furnace.
また本発明の第2の目的は高炉を休風することなく融着
帯の円周バランス崩れを抜本的に改善し、長期に亘って
高炉の燃料比の低下、銑中(Si)のバラツキ減少など
を図れる高炉操業法を提供せんとするものである。The second purpose of the present invention is to drastically improve the circumferential imbalance of the cohesive zone without having to suspend the blast furnace, thereby reducing the fuel ratio in the blast furnace and the variation in pig iron (Si) over a long period of time. The aim is to provide a blast furnace operating method that can achieve these goals.
そもそも高炉の融着帯とは、それぞれ鉱石融着層(以下
、融着層と言う)とコークス層からなり融着層は高炉解
体結果では岩盤上となっており、カスは通り難い層とな
っている。In the first place, the cohesive zone of a blast furnace consists of an ore cohesive layer (hereinafter referred to as the cohesive layer) and a coke layer, and the cohesive layer is found on the bedrock after dismantling the blast furnace, making it a difficult layer for debris to pass through. ing.
一方コークス層は一定の空隙率を確保していることによ
りガスは非常に通り易い層となっている。On the other hand, the coke layer has a certain porosity, so gas can pass through it very easily.
従って融着帯の中の融着層はガスの整流器の役割を果し
ていると云える。Therefore, it can be said that the cohesive layer in the cohesive zone plays the role of a gas rectifier.
極論するならば融着帯形状によって高炉のガス還元効率
は決定され、高炉操業成績の代表的な指数である高炉燃
料比を支配していると云ってもよい。In extreme terms, it can be said that the cohesive zone shape determines the gas reduction efficiency of the blast furnace and controls the blast furnace fuel ratio, which is a representative index of blast furnace operational performance.
高炉操業当事者は。均一な円周バランスのとれた理想的
な融着帯形状を追求して種々アクションをとっていると
云っても過言ではない。Who are the parties involved in blast furnace operation? It is no exaggeration to say that various actions are taken in pursuit of an ideal cohesive zone shape with uniform circumference and balance.
しかし後述するように高炉操業上融着帯円周バランスを
乱す種々の要因があり、長期間に亘って均一な円周バラ
ンスのとれた融着帯を維持することは困難とするところ
であった。However, as will be described later, there are various factors that disturb the circumferential balance of the cohesive zone during blast furnace operation, making it difficult to maintain a uniform circumferentially balanced cohesive zone over a long period of time.
このような融着帯の円周バランスの崩れは、直接、ガス
還元効率の低下、燃料比の上昇を意味するばかりでなく
高炉炉況変動を誘発し銑中[:Si、lは大きくバラツ
キ、良好な溶銑を供給することは困難となる。Such a disruption of the circumferential balance of the cohesive zone not only directly means a decrease in gas reduction efficiency and an increase in the fuel ratio, but also induces fluctuations in the blast furnace furnace conditions, resulting in large variations in [:Si, l] in the pig iron. It becomes difficult to supply good hot metal.
然るにこれまでは抜本的な融着帯形状の調整方法はなく
、上述のような炉況が長期化することが通例であった。However, until now there has been no method for fundamentally adjusting the shape of the cohesive zone, and the above-mentioned furnace conditions have typically been prolonged.
斯様な融着帯の円周バランスの崩れの原因は高炉原料を
炉頂から装入する際に大ベルの偏摩耗等の炉頂装入装置
の欠陥により方向別の装入量が違う場合、鉱石受は金物
直下のレンガ損傷や付着※物生成等により高炉内の内面
プロフィールが不均一となり該損傷部又は該付着物直下
に混合層(コークスと鉱石が混合した層)が生成した場
合、あるいは炉況変動により一時片減り現象(方向別に
荷下りが違った現象を云う)が発生した場合、あるいは
又羽口からの風量バランスが崩れた場合等が考えられ、
その結果、ガスは偏流し炉内ガス還元率ηCO1
の低下を引き起し、銑中(Si)のバラツキを大きくす
る。The cause of such a disturbance in the circumferential balance of the cohesive zone is when the charging amount in each direction is different due to a defect in the top charging device such as uneven wear of the large bell when charging the blast furnace raw material from the top of the furnace. In the case of ore receivers, if the internal profile inside the blast furnace becomes uneven due to damage to the bricks directly under the hardware or the formation of deposits*, and a mixed layer (layer of mixed coke and ore) is formed directly under the damaged area or deposits, Alternatively, there may be a temporary phenomenon of uneven loading due to fluctuations in furnace conditions (a phenomenon in which unloading differs depending on the direction), or the air volume from the tuyeres may be unbalanced.
As a result, the gas flows in a biased manner, causing a decrease in the in-furnace gas reduction rate ηCO1 and increasing the dispersion in the pig iron (Si).
また円周バランスの崩れからガスの偏流が定常的に起る
ことにより、ガス偏流側に付着物が生成したり炉体熱負
荷が異常に高くなったり、装入物の一時的降下不順(以
降荷下り不順と称す)等を引き起し、高炉燃料比上昇の
大きな要因となっている。In addition, due to the steady flow of gas due to an imbalance in the circumference, deposits are formed on the side of the gas drift, the heat load on the furnace body becomes abnormally high, and the charge material temporarily descends irregularly (hereinafter referred to as This is a major factor in the rise in the blast furnace fuel ratio.
このため融着帯の円周バランスの埼−化を図るため、
■ 設備、炉体の本来機能の回復(炉頂装入装置等の修
理調整、付着物除去等による炉内プロフィールの円滑化
)
■ 装入物分布の調整(ムニバブルアーマーのノツチ変
更、装入パターン変更、原料装入物レベル高さの変更等
)
■ 炉下部ガス流れの調整
1本毎の羽口径の調整、1本毎の重油吹込み量の調整
等を実施している。Therefore, in order to increase the circumferential balance of the cohesive zone, we will: ■Restore the original functions of the equipment and furnace body (repair and adjust the furnace top charging device, etc., smooth the furnace profile by removing deposits, etc.) ■ Adjustment of charge distribution (change of munibubble armor notch, change of charging pattern, change of material charge level height, etc.) ■ Adjustment of gas flow in the lower part of the furnace Adjustment of tuyere diameter for each tube, for each tube The amount of heavy oil injection is being adjusted.
しかし従来の方法で融着帯の円周バランスの崩れは充分
に修正することができず、当業者間では確立された技術
の提案が切望されていた。However, conventional methods have not been able to sufficiently correct the circumferential imbalance of the cohesive zone, and there has been a strong desire among those skilled in the art to propose an established technique.
従来休風しない減尺操業を行51態様として提案されて
いるものとして、例えば特公昭42−26377号があ
る。For example, Japanese Patent Publication No. 42-26377 has been proposed as a method of reduced scale operation without air suspension.
しかし、これは装入物を付着物ライン以下に下げ、休風
しないでダイナマイト等の爆薬で付着物除去を目的とす
るものであって、円周バランスを考慮した融着帯調整す
ることについては言及されていない。However, the purpose of this is to lower the charge below the deposit line and remove the deposits using explosives such as dynamite without resting the air, and to adjust the cohesive zone in consideration of the circumferential balance. Not mentioned.
従って、確立された融着帯調整の高炉操業法は提案され
ていないのが現状である。Therefore, at present, no established blast furnace operation method for cohesive zone adjustment has been proposed.
また出願人は上記実状に鑑み、抜本的に融着帯の円周バ
ランスの崩れを改善できる発明を、特許願54−213
36号(特開昭55−115904号)により提案した
。In addition, in view of the above-mentioned circumstances, the applicant has proposed an invention that can fundamentally improve the circumferential imbalance of the cohesive zone in Patent Application No. 54-213.
No. 36 (Japanese Unexamined Patent Publication No. 115904/1983).
この特徴は減尺休風によって融着帯の円周バランスを抜
本的に改善することにある。The feature of this is that the circumferential balance of the cohesive zone is drastically improved by reducing the length of the wind.
然るに該発明では減尺休風するために休風時の炉体放散
熱増の出熱分のコークス比が上昇すること、減尺休風時
の装入物上空胴部はCO及びH2が多量に含まへか2P
頂温度は通常より高く炉頂点火時ガス爆発の危険性があ
ること、減尺休風という外乱条件により送風立上り後、
溶銑温度低下やスリップ、吹抜けが伴う可能性があり、
熱量調整が困難であること等の減尺休風上の間層点があ
る。However, in this invention, due to the reduction in wind shutdown, the coke ratio of the heat output from the increase in heat dissipated from the furnace body during wind shutdown increases, and the cavity above the charge during the reduction in wind shutdown has a large amount of CO and H2. Included in 2P
The top temperature was higher than normal and there was a risk of gas explosion at the top of the furnace, and due to the disturbance condition of reduced wind rest, after the wind started up,
There may be a drop in hot metal temperature, slippage, and blow-through.
There are interlayer points on the downwind where it is difficult to adjust the amount of heat.
本発明は以上の難点を解決することを目的としてなされ
たものであり、その特徴とするところは以下の通りであ
る。The present invention has been made to solve the above-mentioned difficulties, and its features are as follows.
(1)高炉操業法における高炉操業データーを経時的に
把握し、これに対応する過去の推移を基準として各種デ
ーターの一つ、または一つ以上を比較して炉内の異常を
とらえて偏差が設定値以上になったとき減尺し、次いで
上記減尺のときに円周方向の偏差が設定値以内に入るタ
イミングをとらまえて装入物レベルを定常操業時のレベ
ルまで回復させて融着帯を調整することを特徴とする高
炉操業法。(1) Understand the blast furnace operation data over time under the blast furnace operation method, compare one or more of various data with the corresponding past trends as a standard, and identify abnormalities in the furnace and correct deviations. When it exceeds the set value, it is reduced, and then, during the above reduction, when the deviation in the circumferential direction falls within the set value, the charge level is restored to the level during normal operation and fused. A blast furnace operating method characterized by adjusting the belt.
(2)操業データーは、装入物の荷下り、ηeo)鉄中
(Si)或は方向別同一高さレベルのガス圧力、ガス成
分、温度、方向別同一半径レベルの炉頂ガス温度である
特許請求の範囲第1項記載の高炉操業法。(2) Operational data includes unloading of the charge, gas pressure, gas composition, and temperature at the same height level in iron (Si) or direction, and top gas temperature at the same radius level in each direction. A blast furnace operating method according to claim 1.
(3)減尺は減尺レベルに応じた過剰コークス量。(3) Scale reduction is the amount of excess coke according to the scale reduction level.
融着帯レベルに応じた風量、炉頂圧を調整して行う特許
請求の範囲第1項記載の高炉操業法。The method of operating a blast furnace according to claim 1, which is carried out by adjusting the air volume and furnace top pressure according to the cohesive zone level.
(4)減尺はシャフト上端からシャフト中段の間で、或
はシャフト下段から朝顔の間で行う特許請求の範囲第1
項記載の高炉操業法。(4) The reduction is performed between the upper end of the shaft and the middle stage of the shaft, or between the lower stage of the shaft and the morning glory.
Blast furnace operating method as described in section.
ここで装入物を減尺する際に炉内異常をとらえる因子と
して高炉の各種管理要素に限定した理由と、装入物レベ
ルを通常操業レベルに復帰させる際の高炉の各種管理要
素を限定した理由を以下に示す。Here, we will explain why we have limited the various control elements of the blast furnace as factors for detecting abnormalities in the furnace when reducing the burden, and we have limited the various control elements of the blast furnace when returning the burden level to the normal operating level. The reason is shown below.
方向別の同一高さレベルの融着帯が均一であれば方向別
の装入物の還元、溶融滴下が同時に進行するため、その
結果として装入物の荷下りは順調となり、ηeoは安定
し、銑中(Si)のバラツキも少ない。If the cohesive zone is uniform at the same height in each direction, the reduction and melting and dripping of the charge in each direction will proceed at the same time, and as a result, the unloading of the charge will be smooth and ηeo will be stable. , there is little variation in pig iron (Si).
また方向別の同一半径レベルのガス量、ガス温度が一定
のため検出端情報として方向別同一半径レベルの炉頂ガ
ス濃度、方向別同一高さレベルのシャフト圧力値は同一
の値を示すはずである。In addition, since the gas amount and gas temperature at the same radius level in each direction are constant, the detection end information should show the same value for the furnace top gas concentration at the same radius level in each direction and the shaft pressure value at the same height level in each direction. be.
逆に融着帯の円周バランスが崩れると装入物の荷下りは
不順となり、ηcoは低下し、銑中(Si)のバラツキ
が大きくなり、方向別同一半径レベルの炉頂ガス濃度が
違い、方向別同一高さレベルのシャフト圧力値も違った
値を示すことになる。On the other hand, if the circumferential balance of the cohesive zone is disrupted, the unloading of the charge will be irregular, ηco will decrease, the variation in pig iron (Si) will increase, and the top gas concentration at the same radius level in different directions will differ. , the shaft pressure values at the same height level in different directions will show different values.
なお好ましくは以下の管理要素を経時的に把握しこれに
対応する過去の推移を基準として、これらのデータの中
の1つ、又は1つ以上を比較して炉内の異常をとらえた
場合に減尺操業を実施すると更に一層効果的でありより
一層高炉操業の管理を厳しく行なうには必要な条件であ
る。It is preferable to grasp the following management elements over time and use the corresponding past trends as a standard, and compare one or more of these data to detect abnormalities in the furnace. Implementing reduced scale operation is even more effective and is a necessary condition for stricter control of blast furnace operation.
即ち、(イ)同一高さレベルの炉口温度のバラツキ、O
)同一高さレベルのレンガ温度及びステーブ等の炉体温
度のバラツキ、(ハ)方向別同一半径レベルのガス温度
、に)炉頂サーモグラフィーの温度分布、(ホ)炉頂装
入物プロフィール、(へ)支管風量計のバラツキ、(ト
)方向別の炉芯深度測定結果、(7)付着物測定結果。That is, (a) variation in furnace mouth temperature at the same height level, O
) Variation in brick temperature at the same height level and furnace body temperature such as stave, (c) Gas temperature at the same radius level by direction, (e) Temperature distribution in furnace top thermography, (e) Furnace top charge profile, ( f) Variation in branch pipe airflow meters, (g) Core depth measurement results for each direction, (7) Deposition measurement results.
また、装入物を復帰させる際の管理要素を限定した理由
は次の通りである。Furthermore, the reason for limiting the management factors when returning the charge is as follows.
装入物を減尺させても融着帯の円周バランスを精度よく
検知できる検出端は本発明で提案した2種の検出端と炉
体温度やゾンデ等の温度検出端であることに着目した。We focused on the fact that the detection terminals that can accurately detect the circumferential balance of the cohesive zone even when the charge size is reduced are the two types of detection terminals proposed in the present invention and the temperature detection terminals such as furnace body temperature and sonde. did.
即ち装入物を減尺している状態で融着帯の円周バランス
が改善された場合、方向別同一高さレベルのガス圧力の
バラツキが減少し、方向別同一高さレベルのガス成分の
バラツキが減少し、方向別同一高さレベルの温度のバラ
ツキも減少する。In other words, if the circumferential balance of the cohesive zone is improved while reducing the size of the charge, the variation in gas pressure at the same height level in different directions will decrease, and the gas composition at the same height level in different directions will decrease. Variations are reduced, and variations in temperature at the same height level in different directions are also reduced.
また本発明の特徴で減尺レベルに応じた過剰コークス量
調整、融着帯レベルに応じた風量、炉頂圧調整をするこ
とを限定しているが、以下にその理由を述べる。Further, the feature of the present invention is that the amount of excess coke is adjusted according to the scale reduction level, and the air volume and furnace top pressure are adjusted according to the cohesive zone level, and the reason for this will be described below.
従来通常操業時の減尺はダイナマイト爆発による付着物
除去を目的としており、装入物レベルを下げる過程で装
入充填均分の通気抵抗が減少する上、肥大化した付着物
の影響によりガスが瞬時に炉頂に抜げる吹抜げ、大スリ
ップの可能性があり、炉内のヒートバランスが崩れ、溶
銑温度が大巾に低下し冷え込み等の危険性が常にあった
。Conventionally, the purpose of reduction during normal operation was to remove deposits caused by dynamite explosion, and in the process of lowering the charge level, the ventilation resistance of the charging uniformity was reduced, and gas was There was a constant risk of a blowout that could instantly reach the top of the furnace, a large slip, and the heat balance in the furnace would be disrupted, leading to a drastic drop in the temperature of the hot metal and cooling.
しかし、本発明では炉内異常を早期にとらえるため、付
着物肥大等の外乱条件がないことから吹抜け、大スリッ
プを伴うことなく安定炉況を維持し装入物レベルを下げ
る減尺を行うことができ、そのため高炉の出熱量は大巾
に減少し、出熱減分の過剰コークス量は大巾に減少でき
る。However, in the present invention, in order to detect abnormalities in the furnace at an early stage, since there are no disturbance conditions such as enlarged deposits, it is possible to maintain stable furnace conditions without blow-through or large slips, and to perform scale reduction to lower the charge level. As a result, the amount of heat output from the blast furnace can be significantly reduced, and the amount of excess coke due to the reduction in heat output can be significantly reduced.
なおここで云う過剰コークスとは減尺操業期間に熱量調
整として余分に装入するコークスのことを云い、過剰コ
ークス量とは減尺操業1回当りに通常操業時より余分に
装入するコークス量のことを云う。The excess coke referred to here refers to the extra coke charged as a calorific value adjustment during the period of scale reduction operation, and the amount of excess coke refers to the amount of coke charged in excess of the amount during normal operation per scale reduction operation. It refers to
通常操業時に行っていた付着物除去の減尺休風時におけ
る過剰コークス量の決め方は減尺時のスリップ、吹抜け
の熱補償分、送風立上り時に脱落した付着物がガス流れ
を乱すことによるスリップ、吹抜けの熱補償分、脱落し
た付着物を溶解させるために必要な熱補償分、減尺休風
時の炉体放散熱増の熱補償分、減尺することによる減尺
空間部分の装入物保有熱低下による熱補償分等を考慮し
ていた。The method of determining the amount of excess coke during the downtime for removing deposits during normal operation is based on the slip at the time of scale reduction, the thermal compensation for blow-through, the slip due to deposits falling off when the air blows up and disturbs the gas flow. Heat compensation for blow-through, heat compensation necessary to melt fallen deposits, heat compensation for increase in heat dissipated from the furnace during downtime, and charge in the reduced space due to scale reduction. The heat compensation due to the decrease in retained heat was taken into consideration.
従って従来の減尺休風による方法はそれぞれの出熱増の
外乱条件があまりにも多く、多大な過剰コークス量を必
要とするばかりでなく、予想以上に炉況が変動し出熱増
が増加した場合、溶銑温度の著しい低下による冷え込み
が、また反対に予想以上に出熱が少なかった場合は、過
度な溶銑温度高となる。Therefore, in the conventional method of reducing airflow, there are too many disturbance conditions for each increase in heat output, and not only a large amount of excess coke is required, but the furnace conditions fluctuate more than expected, resulting in an increase in heat output. In this case, the hot metal temperature cools due to a significant drop, and conversely, if the heat output is less than expected, the hot metal temperature becomes excessively high.
斯様に従来の減尺休風による過剰コークス量の調整は困
難を極めていた。In this way, it has been extremely difficult to adjust the amount of excess coke using the conventional method of reducing and resting air.
本発明は付着物を肥大化させずに炉内異常を早期にとら
え休風しない減尺操業のため炉況を変動させずに減尺で
きる。The present invention detects abnormalities in the furnace at an early stage without enlarging the deposits, and is capable of downsizing without changing the furnace conditions due to the downsizing operation without wind shutdown.
従って通常操業で行なっている付着物除去の減尺休風で
の過剰コークス量である減尺時のスリップ、吹抜けの熱
補償分、送風立上り時に脱落した付着物がガス流れを乱
すことによるスリップ、吹抜けの熱補償分、脱落した付
着物を溶解させるために必要な熱補償分、減尺休風時の
炉体放散熱増分の熱補償分等の外乱条件による熱補償分
はほとんど必要とすることがなく、減尺することによる
減尺空間分の装入物保有熱低下による熱補償分を考慮す
れば良いことになり、上記の過剰コークス量に対して約
40%〜50%の過剰コークス量で充分であることが分
った。Therefore, there is slip during scale reduction, which is the excess amount of coke during the scale reduction air suspension for removing deposits, which is carried out during normal operation, thermal compensation for blow-through, slip due to deposits falling off when the air blows up, and disturbing the gas flow. Most of the heat compensation due to disturbance conditions is required, such as the heat compensation for blow-through, the heat compensation necessary to melt fallen deposits, and the heat compensation for the increment of heat dissipated from the furnace body during reduced air suspension. Therefore, it is only necessary to consider the heat compensation due to the reduction in heat retention in the charge due to the reduced space due to the size reduction, and the amount of excess coke is about 40% to 50% of the amount of excess coke mentioned above. was found to be sufficient.
また操業が安定することから過剰コークス量を減尺する
装入物レベルに応じて適切に分配することにより溶銑温
度の低下、過度な溶銑温度の上昇が防止でき、安定して
良好な溶銑を供給できることになる。In addition, since the operation is stable, by appropriately distributing the amount of excess coke according to the level of the charge to be reduced, it is possible to prevent a drop in hot metal temperature and an excessive rise in hot metal temperature, thereby stably supplying good hot metal. It will be possible.
例えば減尺操業するには、原料装入物レベルに応じ、お
よび/または炉内容積に応じた適正な過剰コークス量を
装入すればよい。For example, for reduced scale operation, an appropriate amount of excess coke may be charged depending on the raw material charge level and/or the furnace internal volume.
望ましい過剰コークス量の分配の方法は装入物を減尺す
る時に約90%、装入物を定常レベルまで上げる過程に
約10%の過剰コークス量を装入する。A preferred method of distributing the amount of excess coke is to charge about 90% of the excess coke when reducing the charge and about 10% during the course of raising the charge to a steady level.
更に望ましくは装入物を減尺する時の90%分の過剰コ
ークスをシャフト中段までの減尺の場合はそれぞれ一定
割合とし、シャフト下段までの減尺の場合は、シャフト
中段まで約60%シャフト中段からシャフト下段まで約
30%の分配とし、朝顔までの減尺の場合は、シャフト
中段まで50%、シャフト中段からシャフト下段まで2
0%、シャフト下段から朝顔まで20%の分配をするこ
とである。Furthermore, it is preferable that 90% of the excess coke when reducing the charge be reduced to a certain proportion when reducing the length of the charge to the middle stage of the shaft, and when reducing the length of the charge to the lower stage of the shaft, approximately 60% of the excess coke is reduced to the middle stage of the shaft. Approximately 30% is distributed from the middle stage to the bottom of the shaft, and in the case of reduction to morning glory, 50% is distributed from the middle stage of the shaft to the bottom stage of the shaft, and 2 from the middle stage of the shaft to the bottom stage of the shaft.
0%, and 20% from the bottom of the shaft to the morning glory.
なおここで装入物を下げる減尺時に過剰コークス量の大
半を使用し、装入物レベルを定常操業レベルまでの復帰
過程で大巾に減少する理由は、減尺に伴う出熱増の熱補
償を前半に集中して行ない、溶銑温度を充分につげ、そ
の余熱でもって装入物復帰過程の大巾に減少した過剰コ
ークス量を吸収した方が冷え込みの心配がなく、かつ早
期に溶銑温度が正常レベルに戻るということからである
。The reason why most of the excess coke is used during the reduction of the charge, and the charge level is drastically reduced in the process of returning to the normal operation level is due to the increase in heat output due to the reduction of the charge. It is better to concentrate the compensation in the first half, raise the hot metal temperature sufficiently, and use the residual heat to absorb the amount of excess coke that has decreased during the charge recovery process, without worrying about cooling, and to raise the hot metal temperature quickly. This is because it returns to normal levels.
次に本発明で融着帯レベルに応じて風量、炉頂圧を調整
することを限定した理由について以下に述べる。Next, the reason why the present invention limits the adjustment of the air volume and furnace top pressure according to the cohesive zone level will be described below.
前記減尺休風による付着物除去では炉況が不安定でガス
量及びガス温度が変動し融着帯を推定しても精度が悪か
ったが、本発明により安定下で減尺できることから経時
的な融着帯を正確に推定できるようになる。In the method of removing deposits using the above-mentioned scale reduction air break, the furnace conditions were unstable and the gas amount and gas temperature fluctuated, resulting in poor accuracy in estimating the cohesive zone. It becomes possible to accurately estimate the cohesive zone.
その結果融着帯の頂層と原料装入物の距離の接近速度が
異常に速くなる時に装入物が異常に急降下する大スリッ
プが発生するということを知見した。As a result, it was found that when the approaching speed between the top layer of the cohesive zone and the raw material charge becomes abnormally fast, a large slip occurs in which the charge falls abnormally rapidly.
この現象は装入物レベルと融着帯の頂層間で塊状帯充填
物が一番少なく、その距離が異常に接近することにより
ガスは選択的に融着帯頂層部から抜は易くなり、大スリ
ップにつながると思われる。This phenomenon is due to the fact that the bulk zone filling is the least between the charge level and the top layer of the cohesive zone, and as the distance between them becomes abnormally close, it becomes easy for gas to be selectively extracted from the top layer of the cohesive zone. This seems to lead to a slip.
このように減尺巾の装入物レベルと融着帯の頂層間が異
常に接近する徴候を後述するガス圧力等から融着帯を推
定し、融着帯の頂層と装入物レベルの距離が異常に接近
するタイミングをとらまえて風量および/または炉頂圧
を調整すればよい。In this way, the distance between the top layer of the cohesive zone and the charge level is determined by estimating the cohesive zone from the gas pressure, etc., which will be described later, to detect signs that the reduced width charge level and the top layer of the cohesive zone are abnormally close. What is necessary is to adjust the air volume and/or the furnace top pressure by taking the timing when the temperature approaches abnormally.
また上記徴候を把握するには、例えば通気の急速変化、
炉頂温度の急速変化等により行うこともできる。In addition, to understand the above symptoms, for example, rapid changes in ventilation,
This can also be done by rapidly changing the temperature at the top of the furnace.
望ましくは、炉頂圧上昇を先行させ、ガス流速を抑制し
その後風量を内容積当りQ、l Ni/ 1711F1
程度低下させることにより大スリップを防止できる。Desirably, the furnace top pressure is increased in advance, the gas flow rate is suppressed, and the air volume is then reduced to Q, l Ni/1711F1 per internal volume.
Large slips can be prevented by reducing the degree of slippage.
なお、炉頂圧低下のタイミングが遅れた場合は風量低下
を先行して下げるが、内容積当り0.15 Ni/血程
度の風量低下が必要であることも知見している。It should be noted that if the timing of reducing the furnace top pressure is delayed, the air volume is reduced in advance, but it is also known that it is necessary to reduce the air volume by about 0.15 Ni/blood per internal volume.
このように本発明を実施することにより安定した炉況で
減尺させることができ、従って過剰コークス量を大巾に
減少させ、減尺レベルに応じた過剰コークス量の調整が
可能となり、また融着帯形状を時系列的に正確に推定で
きることにより大スリップを防止する風量、炉頂圧調整
が可能となった。By carrying out the present invention in this way, it is possible to reduce the coke under stable furnace conditions, thereby greatly reducing the amount of excess coke, and making it possible to adjust the amount of excess coke according to the level of reduction. By being able to accurately estimate the belt shape over time, it became possible to adjust the air volume and furnace top pressure to prevent large slips.
以上から減尺レベルに応じた過剰コークス量調整、融着
帯レベルに応じた風量、炉頂圧調整をすることを限定し
た。From the above, it was limited to adjusting the amount of excess coke according to the scale reduction level, and adjusting the air volume and furnace top pressure according to the cohesive zone level.
更にまた本発明の特徴として通常操業時に装入物を下げ
る減尺レベルをシャフト上端からシャフト中段までの範
囲と、シャフト下段から朝顔までに分けているのは以下
に述べる理由の通りである。Furthermore, as a feature of the present invention, the reduction level at which the charge is lowered during normal operation is divided into a range from the upper end of the shaft to the middle stage of the shaft, and a range from the lower stage of the shaft to the morning glory for the reason described below.
本発明で提案した2つの検出端を設置していることによ
り、時々刻々に精度よく融着帯の円周バランスを管理で
きるようになった。By installing the two detection ends proposed in the present invention, it has become possible to control the circumferential balance of the cohesive zone with high accuracy from moment to moment.
従って減尺過程で方向別同一高さレベルのシャフト圧力
値、ガス成分、温度の一つまたは一つ以上の偏差が設定
値以内に入る場合は融着帯円周バランスは調整されたと
判断してよく、シャフト下部、あるいは朝顔まで装入物
を減尺させる必要はなくなる。Therefore, if the deviation of one or more of the shaft pressure value, gas composition, and temperature at the same height level in each direction during the reduction process falls within the set value, it is determined that the cohesive zone circumferential balance has been adjusted. Often there is no need to reduce the charge to the bottom of the shaft or even to the morning glory.
以上の理由により融着帯円周バランスの微調整をする場
合は、シャフト上端からシャフト中段までの範囲の減尺
を、さらに融着帯円周バランスを抜本的に改善(融着帯
再構築)する必要がある場合は、既存融着帯の大部分が
存在するシャフト下部から朝顔までの範囲まで減尺する
ことが必要となる。If you wish to fine-tune the circumferential balance of the cohesive zone for the above reasons, you should reduce the range from the upper end of the shaft to the middle of the shaft, and further improve the circumferential balance of the cohesive zone (reconstruction of the cohesive zone). If necessary, it will be necessary to reduce the length from the lower part of the shaft where most of the existing cohesive zone exists to the morning glory.
また本発明によりシャフト中段まで一定時間減尺し融着
帯円周バランスの改善を狙ったが狙い通りに改善されな
い場合は、更にシャフト下部、あるいは朝顔まで段階的
に装入物レベルを下げる方法でもよい。In addition, according to the present invention, we aim to improve the circumferential balance of the cohesive zone by reducing the length up to the middle of the shaft for a certain period of time, but if the improvement is not as desired, it is also possible to reduce the charge level in stages to the lower part of the shaft or to the morning glory. good.
また本発明で提案しているガス圧力計とガス採取装置を
利用し以下の事にも有効に利用できる。Furthermore, the gas pressure gauge and gas sampling device proposed in the present invention can be used effectively for the following purposes.
シャフトから朝顔に集中的に、かつ方向別に設けている
ガス圧力計を利用し減尺時の装入物レベルを精度良く検
知し、減尺中に深指し検尺装置のワイヤー切れ等のトラ
ブル時には強力なバックアップになる。Using gas pressure gauges that are installed centrally from the shaft to the morning glory and in different directions, the charge level during scale reduction can be accurately detected, and in case of problems such as wire breakage of the deep measuring device during scale reduction. It will be a powerful backup.
ガス圧力計が装入物レベルを検知する原理は装入物レベ
ルが当該ガス圧力計を通過すると、当該ガス圧力計の圧
力値は炉頂圧と一致する。The principle by which the gas pressure gauge detects the charge level is that when the charge level passes through the gas pressure gauge, the pressure value of the gas pressure gauge matches the furnace top pressure.
従ってこの原理を利用し、ガス圧力計を直列に集中配置
することにより更に検知精度は向上させることができる
。Therefore, by utilizing this principle and arranging gas pressure gauges in series, the detection accuracy can be further improved.
またシャフトから朝顔の範囲に方向別に設けているガス
分析計を用いて減尺休風時シャフト下部に滞留し易い高
炉ガスの検知にも利用できる。Gas analyzers installed in different directions from the shaft to the morning glory can also be used to detect blast furnace gas that tends to accumulate in the lower part of the shaft during wind down periods.
このようにシャフトから方向別にガス検知することによ
り減尺休風時に発生する可能性のある炉頂ガス爆発の危
険性が防止できる。By detecting gas in each direction from the shaft in this way, it is possible to prevent the risk of a top gas explosion that may occur during reduced air suspension.
なお減尺休風後の炉頂圧はほぼ大気圧と等しいことから
減尺休風時のガス検知はポンプでガスを吸引しガス分析
をする。Note that the pressure at the top of the furnace after a reduction in air is approximately equal to atmospheric pressure, so gas is detected by sucking gas with a pump and gas analysis is performed during the reduction in air.
このように本発明は減尺休風をして融着帯を抜本的に改
善する融着帯再構築方法に比し、容易に、安全に、安価
に、かつ融着帯円周バランスを装入物減尺レベルに応じ
てきめ細かに調整できる画期的な方法と云える。As described above, the present invention can easily, safely, and inexpensively balance the circumference of the cohesive zone compared to the method of reconstructing the cohesive zone, which drastically improves the cohesive zone by reducing the air length. It can be said that this is an innovative method that allows fine adjustments to be made depending on the level of reduction of the material.
次に本発明を図に示す一操業例により更に詳細に説明す
る。Next, the present invention will be explained in more detail with reference to an example of operation shown in the drawings.
第2図と第3図は炉内異常の管理要素であるスリップ回
数(荷下り不順の指標)、ηco (ガス還元効率の
指標)、銑中(Si)のR(銑中(Si)のバラツキの
度合、1日の銑中(Si)の最大〔Si〕から最小(S
i)を引き、その値の月平均)を示した。Figures 2 and 3 show the number of slips (an indicator of poor unloading), ηco (an indicator of gas reduction efficiency), and the R of pig iron (Si), which are management factors for abnormalities in the furnace. degree, from the maximum [Si] to the minimum (S
i) was subtracted to show the monthly average of that value.
第2図と第3図を比較すると明らかに第3図の方が5月
からスリップ回数は増加し、ηeoの低下も激しく、銑
中〔Si)のバラツキも大きくなってきており、融着帯
円周バランスは大きく乱れてきていることを示しており
、融着帯を抜本的に改善するためにシャフト下段から朝
顔までの範囲の減尺する時期と考える。Comparing Figures 2 and 3, it is clear that in Figure 3, the number of slips has increased since May, the decrease in ηeo has been severe, the variation in pig iron [Si] has also increased, and the cohesive zone has increased. This shows that the circumferential balance has become significantly disturbed, and we think it is time to reduce the area from the bottom of the shaft to the morning glory in order to fundamentally improve the cohesive zone.
また第2図のような操業状態は、まだ第3図のようには
至っておらずシャフト上端からシャフト中段までの範囲
の減尺で充分対処可能である。Further, the operational state shown in FIG. 2 has not yet reached the state shown in FIG. 3, and can be sufficiently dealt with by reducing the length from the upper end of the shaft to the middle stage of the shaft.
上記管理要素において好ましい実施態様はスリップが直
近2力月平均より連続して2力月間2.0〜3.0回7
日増加した時、ηeoが直近2力月平均より連続して2
力月間0.3%〜0.5%低下した時、銑中(Si)の
Rが直近2力月より連続して2力月間0.03〜0.0
5%増加した時、の1つ又は1つ以上が発生した時にシ
ャフト上端からシャフト中段までの範囲の間に減尺をし
、融着帯円周バランスの微調整を図ることであり、更に
又スリップが直近2力月平均より連続して2力月間3.
1回以上増加した時、ηeOが直近2力月平均より連続
して2力月間0.6%以上増加した時、銑中(Si)の
Rが直近2力月平均より連続して2力月間0.06%以
上増加した時、第4図に示したように方向別同一半径レ
ベルの炉頂ガス濃度が大きく違う場合、第5図に示した
ように方向別同一高さレベルのシャフト圧力値が大きく
違う場合の1つ又は1つ以上が発生した時にシャフト下
段から朝顔までの範囲の間に減尺をし融着帯円周バラン
スの抜本的な改善を図ることである。A preferred embodiment of the above management factors is that the number of slips is 2.0 to 3.0 times per 2 consecutive months from the average of the most recent 2 months.
When the number of days increases, ηeo is 2 consecutive days higher than the average of the last two months.
When the power decreases by 0.3% to 0.5% per month, the R of pig iron (Si) decreases by 0.03 to 0.0 for two consecutive months from the last two months.
5% increase, when one or more of the above occurs, the scale is reduced between the upper end of the shaft and the middle of the shaft to finely adjust the circumferential balance of the cohesive zone. 3. Slip is higher than the average for the most recent two consecutive months.3.
When ηeO increases more than once, when ηeO increases by 0.6% or more for two consecutive months from the average of the most recent two months, when R of pig iron (Si) increases for two consecutive months from the average of the most recent two months. When the increase is 0.06% or more, if the top gas concentration at the same radius level in each direction differs greatly as shown in Figure 4, the shaft pressure value at the same height level in each direction as shown in Figure 5. When one or more of the following cases occur, the method is to reduce the length between the lower part of the shaft and the morning glory, thereby drastically improving the circumferential balance of the cohesive zone.
なお更に好ましくは以下の管理要素を経時的に把握し、
これに対応する過去の推移を基準として、これらのデー
タの1つ又は1つ以上を比較して炉内異常をとらえた場
合、上記管理基準に達しない場合でも融着帯円周バラン
スの乱れの徴候としてとらえシャフト上端からシャフト
中段までの範囲の間に減尺をするとより一層効果的であ
る。Even more preferably, the following management elements are grasped over time,
If one or more of these data are compared with the corresponding past trends to detect abnormalities in the reactor, even if the above management standards are not met, it is possible to detect disturbances in the cohesive zone circumferential balance. It is even more effective to take this as a symptom and reduce the length between the upper end of the shaft and the middle of the shaft.
(イ)同一高さレベルの炉口温度のバラツキ、(ロ)同
一高さレベルのレンガ温度及びステーブ等の炉体温度の
バラツキ、(ハ)方向別同一半径レベルのガス温度、に
)炉頂サーモグラフィーの温度分布、(ホ)炉頂プロフ
ィールメーターの分布、(へ)支管風量計のバラツキ、
(ト)方向別シャフト微圧、(7)方向別羽口微圧、(
す)方向別炉芯深度測定結果、停)付着物厚さ。(b) Variations in furnace mouth temperature at the same height level, (b) Variations in brick temperature and furnace body temperature such as staves at the same height level, (c) Gas temperature at the same radius level by direction, and (d) Furnace top. Temperature distribution of thermography, (e) distribution of furnace top profile meter, (f) variation of branch pipe airflow meter,
(G) Shaft micro-pressure by direction, (7) Tuyere micro-pressure by direction, (
(1) Core depth measurement results by direction, (3) Thickness of deposits.
次に装入物を下げる減尺レベルに応じた過剰コークス量
を決定する。Next, the amount of excess coke is determined according to the level of reduction of the charge.
この過剰コークス量は従来の付着物除去を目的としたダ
イナマイト爆発による減尺休風に比較し約40〜50%
で充分である。This amount of excess coke is approximately 40 to 50% compared to the conventional method of reducing airflow using dynamite explosion for the purpose of removing deposits.
is sufficient.
つまり付着物による影響の出熱はほとんど考慮する必要
がなく減尺することによる減尺空間分の装入物保有熱低
下による熱補償弁のみを考えれば良い。In other words, there is almost no need to consider the heat output due to the influence of deposits, and it is only necessary to consider the heat compensation valve due to the reduction in heat retained in the charge due to the reduced size space.
ここで1730m’の内容積のA高炉を18mの朝顔ま
で減尺した場合の本発明による過剰コークス量を以下に
試算する。Here, the amount of excess coke according to the present invention when the A blast furnace with an internal volume of 1730 m' is reduced in size to a morning glory of 18 m is estimated below.
(前提)
■ 装入物比熱Cp(coke)=0.31X103k
cal/l−℃
■ 装入物比熱Cp(Ore)=0.22X10”kc
al/l−’C
■ Or e/e oke = 3.40■ コークス
ベース=11t/ch−
■ 減尺空間に入るべきチャージ数=30チャージ
■ 減尺18mまでの装入物平均温度=600℃(1)
1チャージ当りの比熱
11X0.31X10 +11X3.40X0.22
Xi 03=11.64X103(kcal/’C・チ
ャージ)
(2)減尺空間分の装入物保有熱
11.64X10 X600X30=209.5X1
0 kcal
(3)上記熱量補償するためのコークス量を求める。(Assumptions) ■ Charge specific heat Cp (coke) = 0.31X103k
cal/l-℃ ■ Charge specific heat Cp (Ore) = 0.22X10”kc
al/l-'C ■ Or e/e oke = 3.40 ■ Coke base = 11t/ch- ■ Number of charges that should enter the reduction space = 30 charges ■ Average temperature of the charge up to 18m reduction = 600℃ (1)
Specific heat per charge 11X0.31X10 +11X3.40X0.22
Xi 03 = 11.64X103 (kcal/'C charge) (2) Charge heat retention for reduced space 11.64X10 X600X30 = 209.5X1
0 kcal (3) Find the amount of coke for compensating the amount of heat.
C+3AO2=CO+2450 kc al/に9より
コクス灰分を10%としてCoke 1 ton当りの
発熱量は2205X103kcal/lとなる。From C+3AO2=CO+2450 kcal/9, the calorific value per 1 ton of Coke is 2205×103 kcal/l when the coke ash content is 10%.
209.5X106/2205X103=95を従来の
減尺休風による過剰コークス量は、上記計算結果に加え
炉況変動による熱損失増、休風による熱損失増等を加え
る必要があり約190t〜250tの過剰コークス量を
使用していたが、本発明による減尺操業では95tの過
剰コークス量で充分である。209.5 x 106/2205 Although an excess amount of coke was used, an excess coke amount of 95 tons is sufficient for the reduced scale operation according to the present invention.
なお、この過剰コークス量は当然のことながら炉体レン
ガの侵食状況、高炉内容積の違いによって異なる。Note that the amount of excess coke naturally varies depending on the erosion condition of the furnace bricks and the difference in the internal volume of the blast furnace.
減尺する装入物レベルを決定し、それに応じた過剰コー
クス量を決めた後に溶銑温度低下による冷え込みの心配
のない、かつ過度の溶銑温度高にならない装入物レベル
に応じて適正に過剰コークス量を分配する必要がある。After determining the charge level to be reduced and determining the corresponding amount of excess coke, appropriate excess coke is removed according to the charge level without worrying about cooling due to a drop in hot metal temperature and without raising the hot metal temperature excessively. It is necessary to distribute the amount.
第6図と第7図に減尺レベルに応じた望ましい過剰コー
クスの分配をした実施例を示した。FIGS. 6 and 7 show an embodiment in which excess coke is distributed in accordance with the reduction level.
第6図は装入物レベルをシャフト中段までのSL下10
mまでの減尺した例であり、装入物を減尺する時に過剰
コークス量の90%を装入し、残りの10%は装入物レ
ベルの復帰過程で装入し、それぞれ装入物レベルに応じ
て一定割合に分配している。Figure 6 shows the charge level at SL below 10 to the middle of the shaft.
In this example, 90% of the excess coke amount is charged when the charge is reduced in size, and the remaining 10% is charged during the process of returning the charge level, and each charge is It is distributed in fixed proportions depending on the level.
第7図は装入物レベルを朝顔までのSL下18mまで減
尺した例であり、装入物を減尺する時に、過剰コークス
量の90%を装入し、残りの10%は装入物レベルの復
帰過程で装入物レベルに応じて一定割合に分配している
。Figure 7 shows an example in which the charge level is reduced to 18m below the SL to Morning Glory.When reducing the charge level, 90% of the excess coke amount is charged, and the remaining 10% is In the process of restoring the charge level, it is distributed at a fixed ratio according to the charge level.
なお装入物を減尺する時の過剰コークス量の90%の分
配方法は、シャフト中段までは50%、シャフト中段か
らシャフト下段までを20%、シャフト下段から朝顔ま
で20%とそれぞれ分配し、冷え込みを防止し、過度な
溶銑温度高を防止している。The method of distributing 90% of the excess coke when reducing the charge is to distribute 50% to the middle of the shaft, 20% from the middle of the shaft to the lower shaft, and 20% from the lower shaft to the morning glory. This prevents cooling and excessively high hot metal temperature.
次に減尺操業時の風量、炉頂圧について第6図、第7図
に示した実施例に基づき説明する。Next, the air volume and furnace top pressure during reduced scale operation will be explained based on the embodiment shown in FIGS. 6 and 7.
本発明による減尺操業は安定炉況を維持できることから
コンピューターに入力された検出端を基に融着帯形状は
時々刻々に精度よく推定される。Since the scale reduction operation according to the present invention can maintain stable reactor conditions, the shape of the cohesive zone can be accurately estimated moment by moment based on the detection end input into the computer.
第6図と第7図に示したように装入物レベルと融着帯の
頂層間の距離が異常に速く接近する徴候をとらまえて炉
頂圧を先行させて上昇し、炉内ガス流速を抑制させ、更
にその後に内容積当りの風量を0. I Nrrt/
171E11減少させ、スリップ等の炉況変動を防止し
ている。As shown in Figures 6 and 7, in response to signs that the distance between the charge level and the top layer of the cohesive zone is approaching abnormally quickly, the furnace top pressure is increased in advance, and the gas flow rate in the furnace is increased. After that, the air volume per internal volume is reduced to 0. I Nrrt/
171E11 to prevent fluctuations in furnace conditions such as slips.
このようにきめ細かな調整により安定炉況下の減尺操業
が可能となる。Such fine-grained adjustments enable reduced-scale operation under stable reactor conditions.
安定下で目的とする減尺レベルまで装入物を下げた状態
で本発明で提案した2種の検出端と炉体温度やゾンデ等
の温度検出端を利用し時々刻々にそれぞれの円周バラン
スを確認すると共にガス灰中Zn、スラグ中のアルカリ
量の分析も時系列的に測定する。With the charge lowered to the desired reduction level under stable conditions, the circumferential balance of each is measured moment by moment by using the two types of detection terminals proposed in this invention and temperature detection terminals such as furnace body temperature and sonde. In addition to confirming this, the amount of Zn in the gas ash and the amount of alkali in the slag will also be analyzed over time.
第8図に示したように同一高さレベルのガス圧力のバラ
ツキが減少した時、同一高さレベルのガス成分のバラツ
キが減少した時、同一高さレベルのステーブ温度のバラ
ツキが減少した時、高炉灰中Zn量が減少し始めた時、
スラグ中アルカリ量が減少し始めた時の1つ又は1つ以
上が減少したタイミングをとらまえて融着帯円周バラン
スの改善がなったことを確認し、あるいは付着物の脱落
が減少してきたことを確認し、装入物レベルを定常操業
時レベルまで回復させる。As shown in Fig. 8, when the variation in gas pressure at the same height level is reduced, when the variation in gas composition at the same height level is reduced, when the variation in stave temperature at the same height level is reduced, When the amount of Zn in blast furnace ash started to decrease,
It was confirmed that the circumferential balance of the cohesive zone had improved, or that the amount of deposits falling off had decreased, taking into consideration the timing when one or more of the alkali levels in the slag started to decrease. Confirm that this is the case and restore the charge level to the normal operating level.
またここで本発明による減尺操業を実施するために方向
別にシャフトから朝顔にかげ圧力計と、ガス捕集装置を
第9図のように設置することを提案する。In addition, in order to carry out the scale reduction operation according to the present invention, it is proposed to install shaded pressure gauges and gas collection devices from the shaft to the morning glory in each direction as shown in FIG.
すなわち、高炉において円周方向の少なくとも2力所以
上の位置にガスセンサーおよび/または圧力センサーを
設け、且つシャフトから朝顔の間に複数段設けると共に
、炉の下方向に向って上記設置段数を増加したものであ
る。That is, gas sensors and/or pressure sensors are installed at at least two pressure points in the circumferential direction of the blast furnace, and multiple stages are installed between the shaft and the morning glory, and the number of installed stages increases toward the bottom of the furnace. This is what I did.
なおこの理由は、減尺操業時に原料装入物レベルを下げ
ることにより、融着帯の円周バランスの均一性を正確に
検知するために必要である。The reason for this is that it is necessary to accurately detect the uniformity of the circumferential balance of the cohesive zone by lowering the raw material charge level during reduced scale operation.
これは減尺することにより装入物レベル以上に空洞部が
形成されて、上記検出端の一部が露呈して機能を半減す
ることによる。This is because, by reducing the size, a cavity is formed above the charge level, exposing a portion of the detection end and reducing its function by half.
ガス圧力計取出口は、従来高炉に既設されている圧力計
取出口と全く同じ構造で良く、第10図に示す如く普通
の鋼管1にフランジ2を溶接し、そのフランジ2をポル
ト3で鉄皮に固定し、鋼管1からガスを導入し圧力を測
定する。The gas pressure gauge outlet may have the same structure as the pressure gauge outlet conventionally installed in blast furnaces.As shown in Fig. 10, a flange 2 is welded to an ordinary steel pipe 1, and the flange 2 is welded with a port 3. It is fixed to the skin, gas is introduced from the steel pipe 1, and the pressure is measured.
測定された方向別の圧力側は各段別に円周のバラツキを
比較演算するコンピューター4に入力し、一定時間毎に
印字する。The measured pressure side in each direction is input to a computer 4 that compares and calculates the variation in circumference for each step, and is printed out at regular intervals.
又ガス捕集装置の取出口も第11図に示したようにガス
圧力計取出口と全く同じ構造で良い。Further, the outlet of the gas collection device may have the same structure as the outlet of the gas pressure gauge, as shown in FIG.
鋼管5からガスを導入しガスクロマトグラフィー分析計
6で方向別にガス分析する。Gas is introduced through a steel pipe 5 and analyzed by a gas chromatography analyzer 6 in each direction.
測定された方向別のガス分析を各段別に円周バラツキを
比較演算するコンピューター6に入力し、一定時間毎に
印字する。The measured gas analysis for each direction is input to a computer 6 that compares and calculates the circumferential variation for each step, and is printed out at regular intervals.
次に本発明の実施例について説明する。Next, examples of the present invention will be described.
実施例 1 融着帯円周バランスの微調整の実施例。Example 1 Example of fine adjustment of cohesive zone circumferential balance.
1730m”の炉容を有するA高炉でのスリップ、ηe
o、銑中(Si)R″の推移を直近2力月平均と比較し
た結果、スリップは連続して2力月間1回増加し、ηe
oは連続して2カ月間0.2%低下し、銑中(Si)の
豆が連続して0.04%、0.05%と上昇した。Slip in A blast furnace with a furnace volume of 1730 m'', ηe
As a result of comparing the trends in pig iron (Si) R″ with the average of the last two months, the slip increased once in two consecutive months, and ηe
o decreased by 0.2% for two consecutive months, and beans in pig iron (Si) increased by 0.04% and 0.05% consecutively.
銑中(Si)のRが管理基準以上に上昇したことから融
着帯円周バランスの微調整が必要と判断し、装入物レベ
ルをシャフト上段であるSL下6mまで減尺することに
し過剰コークス量を減尺空洞分の装入物保有熱量の低下
として約30を装入することにした。Since the R of the pig iron (Si) had increased above the control standard, it was determined that fine adjustment of the circumferential balance of the cohesive zone was necessary, and the charge level was reduced to 6 m below the SL, which is the upper stage of the shaft. It was decided to charge about 30 coke to reduce the amount of heat retained by the charge due to the reduced size of the cavity.
過剰コークスの分配は基準通り減尺過程時に90%、減
尺復帰時に10%とし減尺過程の90%の分配量はそれ
ぞれ装入物レベルに応じて一定割合とした。As per the standard, excess coke was distributed at 90% during the scale reduction process and 10% at the time of return to scale reduction, and the 90% distribution amount during the scale reduction process was set at a fixed ratio depending on the charge level.
また減尺前の風量は融着帯頂層レベルが装入物レベルを
減尺させた状態でも急速に接近しないので減尺前と同じ
く内容積当り1.25 Nm”/ mj!lの一定とし
、炉頂圧も一定とした。In addition, the air volume before size reduction is constant at 1.25 Nm''/mj!l per internal volume as before size reduction, since the cohesive zone top layer level does not approach rapidly even when the charge level is reduced. The furnace top pressure was also kept constant.
減尺6mに達した時点で約5時間そのままの減尺レベル
で保持した結果、ガス圧力計の同一高さレベルのバラツ
キ(同一高サレベルの最大ガス圧カー最小ガス圧力)が
シャフト下段で150t/cWLから7or/ct炉腹
で120ft/cdから60t/cIILまで減少した
ことから融着帯の円周バランスは改善されたと判断し装
入物レベルを元の通常操業レベルまで復帰した。When the scale reduction reached 6 m, it was maintained at the same scale reduction level for about 5 hours, and as a result, the variation of the gas pressure gauge at the same height level (maximum gas pressure car minimum gas pressure at the same height level) was 150 t/min at the bottom of the shaft. Since cWL decreased from 120ft/cd to 60t/cIIL at 7or/ct furnace belly, it was judged that the circumferential balance of the cohesive zone had been improved, and the charge level was returned to the original normal operating level.
その結果、スリップは解消し、翌月のηeoは前月に比
し0.4%向上し、銑中(Si)の豆は0.05%低下
した。As a result, the slip was resolved, and ηeo for the next month improved by 0.4% compared to the previous month, while beans in pig iron (Si) decreased by 0.05%.
なお減尺操業はスリップもなく極めて順調に推移し溶銑
温度は2tapのみ1510℃台の若干高目であったが
Btap 日取IJ1490〜1500℃の正常レベル
に戻った。Incidentally, the scale reduction operation proceeded extremely smoothly with no slip, and the hot metal temperature was slightly high at 1510°C only at 2 taps, but returned to the normal level of 1490 to 1500°C per day at Btap IJ.
実施例 2 融着帯円周バランスの抜本的な調整の実施例。Example 2 Example of drastic adjustment of cohesive zone circumferential balance.
1730m”の炉容を有するA高炉でのスリップ。Slip in A blast furnace with a furnace capacity of 1730 m''.
ηeo、銑中(Si)Rの推移を直近2力月平均と比較
した結果、スリップは連続して2力月間3回増加し、η
co は連続して2力月間0.5%、0.6%と低下し
、銑中(Si)のRは連続して2力月間0.06%上昇
した。As a result of comparing the trends in ηeo and pig iron (Si) R with the average of the last two months, slip increased three times in two consecutive months, and η
co continuously decreased by 0.5% and 0.6% for two months, and R of pig iron (Si) increased by 0.06% for two months.
また方向別同一半径レベルの炉頂ガスのηeo は炉壁
サイドで1.5%の違い、かつシャフト上段の同一高さ
レベルの東西方向のバラツキも1501/cr/Lも違
うことから融着帯の円周バランスは大きく崩れたと判断
し装入物レベルを炉腹までのSL下16mの減尺を実施
した。Furthermore, the ηeo of the furnace top gas at the same radius level in each direction differs by 1.5% on the furnace wall side, and the dispersion in the east-west direction at the same height level at the top of the shaft also differs by 1501/cr/L, so the cohesive zone It was determined that the circumferential balance of the reactor had been significantly disrupted, and the charge level was reduced by 16 m below the SL to the reactor belly.
過剰コークス量は減尺空間分の装入物保有熱量の低下と
して約85を装入することにした。The amount of excess coke was decided to be approximately 85% as a reduction in the amount of heat retained by the charge due to the reduced size space.
過剰コークスの分配は基準通り減尺過程に90%を装入
し、残りの10%は装入レベルの復帰過程で装入物レベ
ルに応じて一定割合に分配した。As for the distribution of excess coke, 90% was charged in the reduction process as per the standard, and the remaining 10% was distributed in a fixed proportion according to the charging level in the process of restoring the charging level.
なお装入物を減尺する時の過剰コークス量の90%の分
配方法はシャフト中段までは60%、シャフト中段から
シャフト下段まで20%、シャフト下段から朝顔までを
20%とそれぞれ分配した。The method of distributing 90% of the excess coke amount when reducing the charge was 60% to the middle of the shaft, 20% from the middle of the shaft to the lower shaft, and 20% from the lower shaft to the morning glory.
また減尺前の風量は内容積当り1.20 N7F+”/
ruinで、炉頂圧は0.80kg/cI/lで操業し
ていたが、減尺13mの所で装入物レベルと融着帯頂層
間の距離が異常に早く接近する徴候がみられたので直ち
に炉頂圧をo、90kg/crlまで上げ、その3分後
に内容積当りの風量を0.05 Nm”/arm減少し
、その2分後に更に風量を0.05 Nm”/l1m減
少させた。In addition, the air volume before reduction is 1.20 N7F+”/inner volume.
run, the furnace was operated at a top pressure of 0.80 kg/cI/l, but there were signs that the distance between the charge level and the top layer of the cohesive zone was approaching abnormally quickly at a reduction of 13 m. Therefore, the furnace top pressure was immediately increased to 90 kg/crl, and 3 minutes later, the air volume per internal volume was decreased by 0.05 Nm"/arm, and 2 minutes after that, the air volume was further decreased by 0.05 Nm"/1 m. Ta.
減尺16mの所で約1時間保持した結果朝顔の方向別同
一高さレベルの00%のバラツキが約1.5%減少した
ことを確認し装入物レベルを元の通常操業レベルまで復
帰した。As a result of holding for about 1 hour at a reduced scale of 16 m, it was confirmed that the variation in the same height level of morning glories in different directions was reduced by about 1.5%, and the charge level was returned to the original normal operation level. .
その結果中さなスリップは若干あったものの減尺前後の
溶銑温度の最低レベルは1480℃、最高温度は152
0’C3tap続いたが、その後正常レベルの1490
〜1500’Cまで戻った。As a result, although there were some small slips, the minimum level of hot metal temperature before and after scale reduction was 1480℃, and the maximum temperature was 152℃.
0'C3tap continued, but then normal level of 1490
It returned to ~1500'C.
なお、その結果、スリップはほとんど解消し、翌月のη
co は前月に比し、0.6%向上し、銑中(Si、l
の豆は0.06%低下し、燃料比は41#/l−p低下
した。As a result, the slip was almost eliminated, and the following month's η
co improved by 0.6% compared to the previous month;
beans decreased by 0.06% and the fuel ratio decreased by 41 #/l-p.
なおA高炉はシャフト中段、シャフト下段、炉腹、朝顔
レベルの各部位に4方向別に3段ずつシャフト圧力計と
、シャフトガス圧力計を配置している高炉である。Incidentally, the A blast furnace is a blast furnace in which shaft pressure gauges and shaft gas pressure gauges are arranged in three stages in each of four directions at each location: the middle stage of the shaft, the lower stage of the shaft, the furnace belly, and the morning glory level.
実施例 3 融着帯円周バランス微調整の実施例。Example 3 Example of fine adjustment of cohesive zone circumference balance.
1150m”の炉容を有するB高炉でのスリップ。Slip in a B blast furnace with a furnace capacity of 1150 m''.
ηeo、銑中(Si)Rの推移を直近2力月平均と比較
した結果、ηeo、銑中(S i )Rはほとんど変わ
らないが、スリップは連続して2力月間0.5回/日増
加し、炉口温度のバラツキも上昇傾向となっているため
、融着帯微調整の基準以下であったが円周バランスは若
干崩れたと判断しシャフト上端までのSL下5000%
までの減尺をすることにした。Comparing the trends in ηeo and pig iron (Si)R with the averages for the most recent two months, it was found that ηeo and pig iron (Si)R remained almost unchanged, but the slip rate continued to increase by 0.5 times/day in two consecutive months. As the temperature at the furnace mouth increased and the variation in furnace mouth temperature also tended to rise, it was determined that although it was below the standard for fine adjustment of the cohesive zone, the circumferential balance was slightly disrupted, and the SL was adjusted to 5000% below the shaft to the top end.
I decided to reduce the size to .
過剰コークス量は減尺空洞分の装入物保有熱量の低下と
して約20tを装入し過剰コークス量の分配は前述した
基準と全く同じようにした。Approximately 20 tons of excess coke was charged as a reduction in the heat capacity of the charged material due to the reduced size cavity, and the distribution of the excess coke was made in exactly the same manner as the above-mentioned criteria.
減尺の過程で融着帯頂層レベルと原料装入物距離は10
mから8mまでほぼ一定速度で接近したため内容積当り
の風量、炉頂圧共にそれぞれ0、13 Nm/cr?t
、 0.85kg/at/iと一定とした。In the process of reduction, the cohesive zone top layer level and the raw material charge distance are 10
Since the furnace approached from m to 8 m at a nearly constant speed, the air volume per internal volume and furnace top pressure were 0 and 13 Nm/cr, respectively. t
, was kept constant at 0.85 kg/at/i.
SL下5000mmまで減尺した後、約6時間そのまま
保持後、シャフト下段レンガ温度の方向別のバラツキ(
最大温度−最小温度)が220℃から115℃まで低下
、かつ、朝顔レンガ温度の方向別のバラツキも150℃
から95℃まで低下したので融着帯の円周バランスは改
善されたと判断し、装入物レベルを元の通常操業レベル
まで復帰した。After reducing the length to 5000mm below the SL and holding it as it is for about 6 hours, the temperature of the lower shaft bricks was determined by direction (
The maximum temperature - minimum temperature) decreased from 220℃ to 115℃, and the variation in temperature of morning glory bricks by direction was also 150℃.
It was determined that the circumferential balance of the cohesive zone had been improved, and the charge level was returned to the original normal operating level.
減尺操業中はスリップもなく順調に推移し、溶銑温度1
480〜1510℃までと安定して推移し、スリップは
ほとんどなくなった。During the scale reduction operation, the operation progressed smoothly without slipping, and the hot metal temperature was 1.
The temperature remained stable at 480 to 1510°C, with almost no slippage.
以上の通り本発明の採用により以下次の様な効果を奏す
ることができる。As described above, by adopting the present invention, the following effects can be achieved.
1 融着帯円周バランスの微調整。1 Fine adjustment of the cohesive zone circumferential balance.
シャフト上部あるいはシャフト中部までの減尺の場合、
装入物原料の充填物が減少するに伴い、塊状帯(融着帯
上のコークスと鉱石の部分)部分は減少し、塊状帯部分
での上部ガス拡散が減少し高炉ガスは中心流指向となる
。In the case of reduction to the top or middle of the shaft,
As the loading of the raw material for the charge decreases, the lump zone (the part of coke and ore above the cohesive zone) decreases, the upper gas diffusion in the lump zone decreases, and the blast furnace gas becomes central flow oriented. Become.
従って頂層レベルがある方向に偏っている場合、頂層な
中心部へ微調整が可能となる(第1図イ)。Therefore, if the top layer level is biased in a certain direction, fine adjustment can be made to the center of the top layer (FIG. 1A).
2 融着帯円周バランスの抜本的な調整。2. Drastic adjustment of the circumferential balance of the cohesive zone.
シャフト下部あるいは朝顔までの減尺の場合、既存融着
帯レベル以下に減尺することにより、既存の円周バラン
スの崩れた融着帯とは全く異なる均一な融着帯が再構築
される。In the case of reduction to the lower part of the shaft or to the morning glory, by reducing the length below the level of the existing cohesive zone, a uniform cohesive zone, which is completely different from the existing cohesive zone with an unbalanced circumference, is rebuilt.
従って従来あったガスの偏流はなくなりηCOは大幅に
向上する(第1図口)。Therefore, the conventional gas drift is eliminated and ηCO is significantly improved (Fig. 1).
3 減尺操業の安定化。3. Stabilization of reduced scale operations.
炉内異常を早期にとらえ休風をしないで装入物レベルを
下げる減尺操業をすること、融着帯レベルに応じた風量
、炉頂圧を調整していることから吹抜けやスリップを伴
うことなく安定炉況下で減尺操業ができる。By detecting abnormalities in the furnace early and performing reduced-scale operation to lower the charge level without taking a wind break, and adjusting the air volume and furnace top pressure according to the cohesive zone level, blow-by and slipping may occur. Reduced scale operation can be performed under stable reactor conditions.
4 過剰コークス量の大巾減少。4 Significant reduction in excess coke amount.
上記の如く安定炉況下で減尺操業ができることにより、
過剰コークス量は従来の減尺休風に比し約40〜50%
まで大巾に減少でき大巾なコスト低減となる。As mentioned above, by being able to perform reduced scale operation under stable reactor conditions,
The amount of excess coke is approximately 40-50% compared to the conventional reduced-scale wind rest.
This results in a significant cost reduction.
5 冷え込み防止、過度な溶銑温度高防止。5 Prevents cooling and excessively high hot metal temperature.
安定炉況下で減尺できること、休風をしない減尺操業で
あること、装入物レベルに応じた過剰コークス量を分配
していること等から冷え込みの心配がなく、過度な溶銑
温度高も防止できる。There is no need to worry about cooling, and there is no need to worry about excessively high hot metal temperature because it can be reduced under stable furnace conditions, it is a reduced-scale operation without wind breaks, and the amount of excess coke is distributed according to the charge level. It can be prevented.
6 減尺下における融着帯円周バランスの正確な検知、
減尺装入物レベルの検知、減尺休風時の炉頂ガス爆発防
止。6 Accurate detection of cohesive zone circumferential balance under reduced scale,
Detects the level of reduced charge and prevents top gas explosion during downtime.
本発明によるシャフトから朝顔にかけて集中的に設置し
た圧力計及びガス採取装置を設けたことにより、減尺下
における融着帯円周バランスを正確に検知及び管理がで
きるようになった。By providing the pressure gauge and gas sampling device centrally installed from the shaft to the morning glory according to the present invention, it has become possible to accurately detect and manage the circumferential balance of the cohesive zone under reduced scale.
なお、ガス圧力計を方向別シャフトから朝顔に集中的に
設けることにより精度の良い方向別の減尺した装入物レ
ベルを検知でき、かつ又、ガス捕集装置を方向別にシャ
フトから朝顔にかげ設置することから減尺休風後のシャ
フト下部に滞留し易い高炉ガスを検知することにも利用
でき、減尺休風時の炉頂ガス爆発の危険性は防止できる
。In addition, by centrally installing gas pressure gauges from the shaft to the morning glory, it is possible to detect the reduced charge level in each direction with high accuracy. Since it is installed, it can also be used to detect blast furnace gas that tends to stay in the lower part of the shaft after a reduction in wind shutdown, and the risk of a top gas explosion during a reduction in wind shutdown can be prevented.
7 付着物の除去。7. Removal of deposits.
装入物原料を減尺する過程で、あるいは通常レベルの復
帰過程で、付着物に装入物原料を衝突させる効果により
付着物脱落が期待できる。In the process of reducing the size of the charge material or in the process of returning to the normal level, it is expected that the deposits will come off due to the effect of colliding the charge material with the deposits.
従って減尺休風後の荷下りは炉内のワーキングプロフィ
ールが円滑になり装入物の荷下りが順調となる。Therefore, the working profile inside the furnace becomes smooth during unloading after the wind down is reduced, and the unloading of the charge goes smoothly.
8Zn、アルカリの高炉内からの排出、付着物の生成、
成長抑制、炉況の安定。8 Zn, alkali discharge from blast furnace, formation of deposits,
Suppression of growth and stabilization of furnace conditions.
各高炉の解体結果によるとZn 、アルカリの炉内濃縮
温度は前者で400〜1100℃、後者で800〜13
00°Cである。According to the disassembly results of each blast furnace, the in-furnace concentration temperature of Zn and alkali is 400-1100℃ for the former and 800-130℃ for the latter.
It is 00°C.
シャフト上段からシャフト中段までの温度は200〜8
00℃、シャフト下段から朝顔までの温度は900〜1
500℃であることから減尺レベルに応じて、Zn 、
アルカリの一部は蒸発して高炉ガス灰と共に炉内から排
出される。The temperature from the upper shaft to the middle shaft is 200-8.
00℃, temperature from the bottom of the shaft to the morning glory is 900-1
Since the temperature is 500°C, depending on the scale reduction level, Zn,
A portion of the alkali evaporates and is discharged from the furnace together with blast furnace gas ash.
また脱落した付着物の主成分はZn 、アルカリの酸化
物であり、これも又高温にさらされ高炉ガス灰、あるい
はスラグを通して高炉内から排出でき、付着物生成成長
を抑制できる。The main components of the deposits that have fallen off are Zn and alkali oxides, which are also exposed to high temperatures and can be discharged from the blast furnace through blast furnace gas ash or slag, thereby suppressing the formation and growth of deposits.
またアルカリの循環量が増加するに伴い高炉下部に存在
するコークスが亀裂し細粒化することが知られているが
、本発明により炉内からアルカリが一部排出され循環す
るアルカリ量が減少することによりコークスの細粒化は
減少し、通気は改善され炉況安定につながる。It is also known that as the amount of alkali circulating increases, the coke present in the lower part of the blast furnace cracks and becomes finer. However, with the present invention, some of the alkali is discharged from the furnace, reducing the amount of alkali circulating. This reduces coke fineness, improves ventilation, and stabilizes furnace conditions.
9 銑中(Si)のバラツキ低下。9. Reduced variation in pig iron (Si).
融着帯円周バランスが均一となることから方向別の融着
層の溶は落ちレベルが均一となり、溶銑成分は安定し良
好な溶銑を供給できる。Since the circumferential balance of the cohesive zone is uniform, the melting of the cohesive layer in each direction is reduced and the level is uniform, the hot metal components are stable, and good hot metal can be supplied.
また銑中(Si)のバラツキが減少できることから銑中
(Si)の低下が可能となる。Furthermore, since the dispersion of the pig iron (Si) can be reduced, it is possible to lower the pig iron (Si).
10 炉体熱負荷の軽減。10 Reduction of furnace heat load.
融着帯円周バランス崩れによるガス偏流が防止できるこ
とにより炉体熱負荷が低下し、炉体放散熱も低下する。By being able to prevent gas drift due to an imbalance in the circumference of the cohesive zone, the heat load on the furnace body is reduced, and the heat dissipated from the furnace body is also reduced.
この結果、本来の炉体機能維持が長期に亘り可能となり
、かつ炉体放散熱誠により高炉の出熱は減少する。As a result, it becomes possible to maintain the original furnace function for a long period of time, and the heat output of the blast furnace is reduced due to the heat dissipation of the furnace body.
11 ηeoの上昇、燃料比低下。11 Increase in ηeo, decrease in fuel ratio.
以上の1〜10の効果が相俟って燃料比は大巾に低減で
きると同時にまたηeoは上昇し長期に亘り高能率な操
業が維持できる。The above-mentioned effects 1 to 10 can be combined to greatly reduce the fuel ratio, and at the same time, increase ηeo, making it possible to maintain highly efficient operation over a long period of time.
第1図イ2口は融着帯微調整及び融着帯再構築の概念図
、第2図から第11図は本発明に係る一実施例を示すも
ので、第2図は融着帯微調整をする時の炉内異常を表わ
すスリップ回数、ηco。
(Si、IRの例を示す図、第3図〜第5図は融着帯再
構築をする時の炉内異常を表わすスリップ回数、ηco
、(Si )R,炉頂ガス濃度、方向別のシャフト圧力
分布の例を示す図、第6図は融着帯微調整する際の風量
、炉頂圧、過剰コークス量の調整方法を示す図、第7図
は融着帯再構築をする際の風量、炉頂圧、過剰コークス
量の調整方法を示す図、第8図イ2口、ハは融着帯の円
周バランスの改善状況を示す図、第9図は方向別に設け
たガス圧力計とガス採取装置のフローを示した図、第1
0図はガス圧力計の取出口とガス圧力比較演算器を表わ
す図、第11図はガス成分採取装置の取出口とガス成分
比較演算器を表わす図である。Figure 1A2 shows a conceptual diagram of cohesive zone fine adjustment and cohesive zone reconstruction, Figures 2 to 11 show an embodiment of the present invention, and Figure 2 shows the cohesive zone fine adjustment. The number of slips, ηco, which indicates an abnormality in the furnace during adjustment. (Figures showing examples of Si and IR, Figures 3 to 5 are the number of slips representing abnormalities in the furnace when reconstructing the cohesive zone, ηco
, (Si)R, furnace top gas concentration, and a diagram showing an example of shaft pressure distribution according to direction. Figure 6 is a diagram showing a method of adjusting air volume, furnace top pressure, and excess coke amount when finely adjusting the cohesive zone. , Figure 7 is a diagram showing how to adjust the air volume, furnace top pressure, and excess coke amount when reconstructing the cohesive zone. Figure 9 is a diagram showing the flow of gas pressure gauges and gas sampling equipment installed in different directions, Figure 1.
0 is a diagram showing the outlet of the gas pressure gauge and the gas pressure comparison calculator, and FIG. 11 is a diagram showing the outlet of the gas component sampling device and the gas component comparison calculator.
Claims (1)
握し、これに対応する過去の推移を基準として各種デー
ターの一つ、または一つ以上を比較して炉内の異常をと
らえて偏差が設定値以上になったとき減尺し、次いで上
記減尺のときに円周方向の偏差が設定値以内に入るタイ
ミングをとらまえて装入物レベルを定常操業時のレベル
まで回復させて融着帯を調整することを特徴とする高炉
操業法。 2 操業データーは、装入物の荷下り、ηco、鉄中(
Si)或は方向別同一高さレベルのガス圧力。 ガス成分、温度、方向別同一半径レベルの炉頂ガス濃度
である特許請求の範囲第1項記載の高炉操業法。 3 減尺は減尺レベルに応じた過剰コークス量。 融着帯レベルに応じた風量、炉頂圧を調整して行う特許
請求の範囲第1項記載の高炉操業法。 4 減尺はシャフト上端からシャフト中段の間で、或は
シャフト下段から朝顔の間で行う特許請求の範囲第1項
記載の高炉操業法。[Claims] 1. Blast furnace operation data in the blast furnace operation method is grasped over time, and one or more of various data are compared based on the corresponding past trends to detect abnormalities in the furnace. When the deviation exceeds the set value, the charge level is reduced, and then the charge level is restored to the level during normal operation by determining the timing when the deviation in the circumferential direction falls within the set value during the above reduction. A blast furnace operating method characterized by adjusting the cohesive zone by adjusting the cohesive zone. 2 Operational data includes unloading of charge, ηco, iron medium (
Si) or gas pressure at the same height level in each direction. The blast furnace operating method according to claim 1, wherein the top gas concentration is at the same radial level for each gas component, temperature, and direction. 3 Scale reduction is the amount of excess coke according to the scale reduction level. The method of operating a blast furnace according to claim 1, which is carried out by adjusting the air volume and furnace top pressure according to the cohesive zone level. 4. The blast furnace operating method according to claim 1, wherein the reduction is performed between the upper end of the shaft and the middle stage of the shaft, or between the lower stage of the shaft and the morning glory.
Priority Applications (1)
| Application Number | Priority Date | Filing Date | Title |
|---|---|---|---|
| JP55014835A JPS5833283B2 (en) | 1980-02-12 | 1980-02-12 | Blast furnace operation method |
Applications Claiming Priority (1)
| Application Number | Priority Date | Filing Date | Title |
|---|---|---|---|
| JP55014835A JPS5833283B2 (en) | 1980-02-12 | 1980-02-12 | Blast furnace operation method |
Publications (2)
| Publication Number | Publication Date |
|---|---|
| JPS56112405A JPS56112405A (en) | 1981-09-04 |
| JPS5833283B2 true JPS5833283B2 (en) | 1983-07-19 |
Family
ID=11872079
Family Applications (1)
| Application Number | Title | Priority Date | Filing Date |
|---|---|---|---|
| JP55014835A Expired JPS5833283B2 (en) | 1980-02-12 | 1980-02-12 | Blast furnace operation method |
Country Status (1)
| Country | Link |
|---|---|
| JP (1) | JPS5833283B2 (en) |
-
1980
- 1980-02-12 JP JP55014835A patent/JPS5833283B2/en not_active Expired
Non-Patent Citations (1)
| Title |
|---|
| STAL IN ENGLISH=1965 * |
Also Published As
| Publication number | Publication date |
|---|---|
| JPS56112405A (en) | 1981-09-04 |
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